Final Accident Report on N420PS


It's always with a heavy heart that I think back to that day in May 2011 where I was told about Lewis University Aviation student Scott Tezak's accident in Florida. In my first write up (See: Lewis University Loses an Aviation Student), I had promised to write more when the final NTSB report was issued. On 11/05/2012 that report finally came out and as promised, the details are below. I will just be posting relevant facts taken from the two reports with almost no commentary.


While there are always important lessons to be learned from them, aviation accidents are always a devastating event for family, friends, and the aviation community.
NTSB Identification: ERA11FA287
14 CFR Part 91: General Aviation
Accident occurred Friday, May 06, 2011 in Spring Hill, FL
Probable Cause Approval Date: 11/05/2012
Aircraft: Czech Sport Aircraft AS Piper Sport, registration: N420PS
Injuries: 1 Fatal.
NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.
The pilot, who had previously provided flight instruction in the light sport airplane to its two principal owners, was flying it at night from Florida to Illinois. The pilot had flown commercially from Illinois to Florida earlier that day and had been offered lodging by the owners on several occasions but declined. The airplane was not approved for night operations due, in part, to a lack of interior lighting. For over an hour after takeoff, on a clear, dark night, the airplane was headed northbound in straight and level flight at 6,500 feet. The pilot, who had been in contact with an air traffic control facility, had been told to switch to a new radio frequency; afterward radar contact was lost and there were no distress calls from the pilot.
The airplane impacted wooded terrain and was mostly consumed by post-impact fire. All flight control surfaces were accounted for at the scene and no preexisting mechanical anomalies were found. There was no evidence of an in-flight fire and no evidence of the pilot attempting to use the whole-airplane ballistic parachute system.
The pilot was found about 1/3 mile away from the wreckage, about 600 feet to the right of the airplane's radar track. Numerous personal items were also located to the right of the airplane's radar track, with heavier items generally closer to the track than the lighter items. Shards of bubble-canopy glass and the canopy frame were found at the airplane's impact site, but no shards were noted in the vicinity of where the pilot or the personal items were found, indicating that the canopy was likely unlatched and open when the pilot and the other items exited the airplane.
Each seat of the two-seat airplane was equipped with a four-point restraint harness, with each harness having four identical belt adjusting mechanisms: two for the risers and two for the seatbelt portion of the harness. Except for a number of small pieces, both harnesses were almost entirely burned. One surviving piece, for adjusting either a riser or a seat belt portion of the harness, had distorted metal and pulled material, consistent with sudden, forceful loading. The top of the pilot's shoulders also exhibited bruising, indicative of a sudden loading while the harness risers were loosely in place. There were no marks on the pilot's frontal area to indicate that the seat belt portion of the harness was buckled at the time of the loading.
Ground testing revealed that access to the back shelf behind the seats would have been difficult to reach if the pilot had not unbuckled the seat belt portion of his restraint harness and loosened the risers. Thus, it is likely that the pilot tried to reach something on the back shelf. Then, at some point afterward, the canopy T-handle likely became unlatched, possibly having been caught by a loose right harness riser or a looped headset wire that plugged in next to the canopy handle. With a dark, noisy cockpit, the pilot likely then inadvertently applied rapid control inputs that resulted right-rolling, negative g-forces of sufficient intensity to eject him and the other personal items.
The National Transportation Safety Board determines the probable cause(s) of this accident to be: The pilot's inadvertent application of control inputs that resulted in rapid, right-rolling, negative g-forces during night cruise flight and his subsequent ejection from the airplane. Contributing to the accident was the pilot's decision to fly at night in an airplane not approved for night flight, his unbuckling of the seat belt portion of the restraint harness, and the inadvertent opening of the airplane’s canopy.
Click on the corresponding link to view the two full reports: Factual or Probable Cause.


By all accounts, Scott Tezak was larger than life and everything you would look for in a friend, family member, and pilot. He leaves behind a mother, father, younger sister, fiancée and a daughter. The very cold nature of an NTSB report often fails to mention that human errors are not just limited to the careless, but to anyone brave enough to venture into the sky. Keep this in mind, and fly safely.

"It is better to pass boldly into that other world in the full glory of some passion than fade and wither dismally with age." - Katie Ziegler, Scott's cousin using a quote to describe Tezak's life
Final Accident Report on N420PS Final Accident Report on N420PS Reviewed by Joe Burlas on November 05, 2012 Rating: 5

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